SUCCESS STORY #1
OPEN HOLE LOGGING UNDER MPD CONDITION ON SEMI-SUBMERSIBLE RIG
Challenge
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Enable safe rig up and allow for accurate depth control during heave compensation
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Maintain borehole pressure through mud system
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Control risk of total loss / sudden kick during logging operations
Solution
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Integrated SMART SUB and grease injection system were used to overcome the RISKS in PMCD conditions
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Provided simultaneous entry points for wireline tool string and drilling mud
Results
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Nine successful logging runs conducted under active pressure control
'Wireline Data Acquisition under Managed Pressure and
Pressurized Mud Cap Drilling Condition – Pushing the Boundaries of Data Acquisition Envelope for Formation Evaluation'
We recently submitted a conference paper on the MPD condition which was presented at the Offshore Technology Conference in Asia.
Now available online.
SUCCESS STORY #2
PIPE RECOVERY OPERATION ON SEMI-SUBMERSIBLE RIG USING SMART SUB
Challenge
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Enable wireline rig up maintaining heave compensation
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Free stuck BHA by a safe pipe recovery operation
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Always maintain full well-control
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Back-off as close as possible to the stuck point
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Verify free pipe
Solution
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The SMART SUB was used to allow wireline entry from the side
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Pad Eye Sub was used to connect the top sheave as part of the BHA and allow for accurate depth measurement during heave compensation
Results
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Successful and safe pipe recovery at the stuck point, while maintaining full well-control and accurate depth measurement
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Eliminated the need for complex rig up of coil tubing lifting frame
SUCCESS STORY #3
PIPE RECOVERY OPERATION USING SMART SUB
Challenge
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Retrieve radioactive sources in horizontal section
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Free stuck BHA by a safe pipe recovery operation
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Always maintain full well-control
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Back-off as close as possible to the stuck point
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Verify free pipe
Solution
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Enabled wireline entry while driller had full control on
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Pumped wireline tool down the horizontal section for radioactive source fishing to release the stuck BHA through the top drive system
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Pulled / rotated / pumped using the SMART SUB – to enable a safe and simplified pipe recovery operation
Results
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Successful back-off operation
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Safe retrieval of radioactive sources
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Achieved two joints above the stuck point resulting in a freed BHA on the first attempt